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HomeMy WebLinkAbout06. (Handout) Presentation on Energy Optimization Project, DP 7320Item 6. (Committee Handout) ENERGY OPTIMIZATION PROJECT DISTRICT PROJECT 7320 ti Engineering and Operations Committee Meeting October 21, 2016 Clint Shima, P.E. Senior Engineer RECENT OPERATION HISTORY • Notice of Violations from BAAQMD in April 2016 for Co ■ Co not continuously monitored (only two year -cycle) ■ Staff reduced power output to stay within compliance • Air emissions test in May and engine tuning by Solar Turbine ■ Warranty letter in August to Solar Turbine • -Two additional testing and tunings to verify engine emission parameters by Solar Turbine ■ Concluded: Engine within specifications 1 PROJECT BACKGROUND • Project initiated for potential treatment plant improvements that increase energy efficiency and decrease emissions • Researched past and new alternatives • Carollo Engineers (Sarwan Wason —original designer) reviewed alternatives (with business case evaluations) • Two improvements identified with quick pay backs: • Improvement 1: CO Emission Reduction • Improvement 2: Energy Optimization • Total estimated project cost $600,000 IMPROVEMENT 1: CO EMISSION REDUCTION CO CATALYST • Allow operation at higher loads • Allows operations more flexibility • Reduce emissions, 50-75%, reduction of CO • Payback period is approximately three years • Installed in ducting 10/25/2016 2 CO CATALYST LOCATION IMPROVEMENT 2: ENERGY OPTIMIZATION EVAPORATIVE COOLER • Carollo Engineers Technical Memorandum • Allows more power generation in summer when peak costs are high • Installed in air inlet room • Payback period calculated at three years 10/25/2016 3 EVAPORATIVE COOLER AT INLET STAFF RECOMMENDATIONS • Authorize General Manager to transfer up to $550,000 this fiscal year for Energy Optimization Project (District Project 7320) • Staff will proceed with design and bid project • Design contract with Carollo Engineers 10/25/2016 4